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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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				I learned a lesson today
			 
			in April i bought a complete 912 motor from a local guy, that motor had some problems and to make it right he gave me a "deal " on a motor that he had stashed away that had 300 miles on it and new heads done by a real reputable shop and he suspected that there was m.c. pistons in it but he wasn't shure. i was excited to Finlay own a Porsche motor having owned many vws and now having a 912 in need of a motor.  considering that this guy has a good reputation in the Porsche community i took his word. in talking to him today,i told him he did not misrepresent anything or sell me something that wasn't what he said it was. he told me everything he knew about the motor. if i had done a compression check i would have found the problem... one of the heads was never torqued, a couple of the bolts were finger tight. this is what has been giving me problems with bad idle/ starting. so now i will take every motor apart that i buy, just to know that it is how it should be. fortunately the machine shop said that the heads would clean up easily and there wasn't any major damage. if this person is reading, i hold nothing against you   | ||
|  12-01-2008, 07:10 PM | 
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| Registered Join Date: Oct 2005 Location: Martinez, CA 
					Posts: 356
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			Got any more pics of the car/motor?
		 
				__________________ 1997 Boxster SOLD 1999 R1100S SOLD 1988 Carrera 3.2 | ||
|  12-01-2008, 08:15 PM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
				 |   this is my first porsche | ||
|  12-02-2008, 06:07 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
				 |    i did the front end last summer, boy that was alot of fun!!!! | ||
|  12-02-2008, 07:37 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
				 |  this was taken when i firs recieved the engine | ||
|  12-02-2008, 07:41 AM | 
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| Registered Join Date: Nov 2006 Location: Charlotte, NC 
					Posts: 1,514
				 | If you would have shown me this picture I could have just told you that two head bolts were loose.. saved you a ton of trouble.   
				__________________ JP '76 911s Ice Green Metallic bone stock | ||
|  12-02-2008, 08:08 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			how can you tell with the tin on???
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|  12-02-2008, 08:41 AM | 
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| Registered Join Date: Nov 2006 Location: Charlotte, NC 
					Posts: 1,514
				 | Think dry sense of humor.  Sorry never been good at jokes.. but I keep tryin. 
				__________________ JP '76 911s Ice Green Metallic bone stock | ||
|  12-02-2008, 10:26 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			i have one of those too, but there are some old guys on here that know more than i do so i have to ask.
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|  12-02-2008, 10:59 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			so if you are troubble shooting dont forget to check the simple things like are the heads on tight
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|  12-09-2008, 11:53 AM | 
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| Zink Racer Join Date: Aug 2005 Location: Spokane WA 
					Posts: 4,017
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			Was his name Larry?  Advertises on Craigslist?  I have a 912 motor from him as well.  He ran it on his bench, we took compression numbers a few times.  Hopefully it's a good motor.  Seemed like a very good guy to deal with.  I have not installed mine as yet, sitting in my shop.  Maybe this winter.
		 
				__________________ Jerry 983 911 SC/Carrera Franken car, 1974 914 Bumblebee, 1970 914-4 | ||
|  12-09-2008, 12:56 PM | 
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			Which head was loose!!
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|  12-09-2008, 03:07 PM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			3/4 was loose and the intake valve on the number two had beeten its way into the seat. the shop weilded and reground the seat.
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|  12-10-2008, 06:57 PM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
				 | Quote: 
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|  12-10-2008, 07:07 PM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			well got the motor back in the car last week and it runs like a new porsche engine should. all is well with the world now. | ||
|  01-21-2009, 06:42 PM | 
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| Zink Racer Join Date: Aug 2005 Location: Spokane WA 
					Posts: 4,017
				 | Quote: 
 
				__________________ Jerry 983 911 SC/Carrera Franken car, 1974 914 Bumblebee, 1970 914-4 | ||
|  01-22-2009, 07:40 AM | 
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| Registered Join Date: Dec 2003 Location: Arapahoe County, Colorado, USA 
					Posts: 9,032
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			If the head nuts weren't torqued, I would question the rod nuts and the flywheel nut. Best, Grady 
				__________________ ANSWER PRICE LIST (as seen in someone's shop) Answers - - - - - - - - - - - - - - - - $0.75 Answers (requiring thought) - - - - $1.25 Answers (correct) - - - - - - - - - - $12.50 | ||
|  01-22-2009, 09:37 AM | 
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| 1966 - 912 - SOLD Join Date: May 2008 Location: oak grove, OREGON 
					Posts: 3,193
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			in thinking about this whole thing in the post, the engine was pulled from a car that had a "little" fire and then put on a shelf for (x) years. the o rings that go on the bottom head nuts were hard and cracking when i removed the heads, and two were pressed very thin. also the head studs were not driven completely into the case there was 1/8 inch of threads showing on almost all of them. those two things were the contributing factors that created the masive compression leak. again make sure what you get is what you think you are getting.
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|  01-28-2009, 02:07 PM | 
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