|
Senior Member
Join Date: Jun 2000
Location: N. Phoenix AZ USA
Posts: 28,977
|
Afternoon update! Loren called me a couple of hours ago and good/bad news. The difficult news is that the ECU had lost BOTH of its grounds to the engine and thats why it was hunting with the RPM's. The air-flow meter had no signal as a result.
Its now been fixed and hopefully will be on its way back towards Phoenix tomorrow. Excellent service and turn-around time and a very reasonable price!! Thanks for the referral everyone!
__________________
2021 Subaru Legacy, 2002 Dodge Ram 2500 Cummins (the workhorse), 1992 Jaguar XJ S-3 V-12 VDP (one of only 100 examples made), 1969 Jaguar XJ (been in the family since new), 1985 911 Targa backdated to 1973 RS specs with a 3.6 shoehorned in the back, 1959 Austin Healey Sprite (former SCCA H-Prod), 1995 BMW R1100RSL, 1971 & '72 BMW R75/5 "Toaster," Ural Tourist w/sidecar, 1949 Aeronca Sedan / QB
|