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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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3.2 rebuild questions
I’m rebuilding my 1987 3.2. It will be a stock rebuild. I have a couple questions for you seasoned rebuilders.
1) should I replace the exhaust side head studs. Are they a problem like the 3.0 liters? 2) I’m planning on using the Cohline brand oil lines available here on Pelican. The cam and tensioner feed lines. Has anyone had issues with them? TIA Last edited by dave7320; 01-22-2018 at 01:28 AM.. |
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Registered
Join Date: Oct 2008
Location: Nash County, NC.
Posts: 8,480
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Replace the bottom row of studs with factory steel.
Oil lines will be good, sometimes they need a smidge of adjusting Lest you forget, the oil scavenge line goes to the inside on the thermostat. If you can’t get the connector off the thermostat, cut diagonally the nut to relieve the threads of aluminum on the thermostat. Bruce |
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Registered User
Join Date: Jan 2018
Posts: 7
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How's the progress of your rebuild?
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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Disassembly is done. Found problems with #4 cylinder. It was leaking oil around the base of the cylinder and looked like the combustion chamber seal was leaking too. The oil control ring was 2 pieces and the intermediate shaft bearings were showing some copper. The crankshaft is straight and in spec. The rods are being rebushed and resized. Cams and rockers show minimal wear.
My head guy found a problem with head #4. It was machined wrong at the factory. It was .006” deeper pocket than the other heads. Effectively making it shorter when torqued. No wonder they head leaked. Intakes guides were toast in the whole motor. Everything else showed low wear. ![]() ![]() ![]() ![]() |
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abit off center
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with one head off that much I'm surprised the cam even turned?
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______________________ Craig G2Performance Twinplug, head work, case savers, rockers arms, etc. |
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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It wasn’t .006” across. It’s was deeper at one end like there was a chip or something under the one sidewhen they machined it at the factory. There are no signs that the motor had been opened before. I will check the cam bores for elongation.
Last edited by dave7320; 02-02-2018 at 07:07 AM.. |
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Under the radar
Join Date: May 2007
Location: Fortuna, CA. On the Lost Coast near the Emerald Triangle
Posts: 7,129
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Kudos to your motor guy for finding that problem with the head. Amazing.
Sounds like the rest of the motor just needs a freshen-up. Good luck.
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Gordon ___________________________________ '71 911 Coupe 3,0L outlawed #56 PCA Redwood Region, GGR, NASA, Speed SF Trackrash's Garage :: My Garage |
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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Picked up the heads yesterday. The intake guide were Were severely worn. Stems on the valves were shot. Three sets of valve springs were weak. So all new valves guides and springs. Today is cleaning parts at work. Then check the cam bores and the new cylinder heights/bores and piston diameters. Ring gaps and ring groove clearances. Not even trusting Mahle’s quality control after finding my head issue. Hehe
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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After spending 4 hours in the parts cleaning tank. Found some wear issues with the cam and rockers. Rockers are heading to cgarr and the cam is going to camgrinder for a regrind. Here are some cam lobe pics.
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Schleprock
Join Date: Sep 2000
Location: Frankfort IL USA
Posts: 16,639
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Mahle didn't make the heads so don't blame them?
![]() I gots a spark plug like that too! ![]() What Craig is saying about the cam housings isn't about the bore dimensions. It's about one head being the wrong height and then when you bolt the housing to the head, it potentially distorts the housing such that the four cam bearing bores are not co-linear. That would make the cam difficult to turn. These cam housings seem to be somewhat of a dimensionally unstable casting. You can check the flatness of the housing's head sealing surface and the valve cover surfaces and you'll rarely find them to be anywhere near flat. Seems a lot of them are slightly "twisted" when they're not mounted on the heads. I suspect when they are mounted to the heads, they straighten out a bit.
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Kevin L '86 Carrera "Larry" |
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Registered
Join Date: Nov 2000
Location: Dallas
Posts: 3,575
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One thing I learned in my rebuild, and in later attempts to address the issue, is the cam oil lines have an issue. The problem is the tube part that inserts into the hollow bolt on the case is about 1/8" too long. This keeps the ferrule from snugging down and actually making a good seal. The simple solution is to grind off about 1/8", making sure to clean it up, then installing as normal. I replaced this 3 times before I finally figured out what the problem was. IIRC John Walker may have noticed this as well. Another, expensive, solution is to order the "Porsche" part that does not have the ferrule pre installed, Its much more expensive and the solution I used solved the problem perfectly.
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Buck '88 Coupe, '87 Cab, '88 535i sold, '19 GLC 300 DD Warren Hall, gone but not forgotten |
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May I ask how many miles were on this engine? I am in the process of doing similar on my 88 with 101K in the coming months and would like to use this as a baseline for what I may encounter inside. looking forward to your progress. Dan.
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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About 65k as far as I know. Bought it used of a guy who did a 3.2 conversation. Hopefully you won’t find this any issues.
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Registered
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Quote:
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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My guess is quality control slipped up on this motor. The exhaust guides were only worn minimal. So there must have been a quality problem with the intakes being so bad at such low mileage. The cam looks like poor oil condition. The bottom end looks like a low mileage motor.
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Quote:
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914 JUNKIE
Join Date: Aug 2007
Location: Willow Grove PA
Posts: 186
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Intermediate shaft bearings were showing copper on this motor.
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Registered
Join Date: Oct 2008
Location: Nash County, NC.
Posts: 8,480
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They all show copper. The tensioners put out lots of running pressure and intermediate shaft bearings suffer but do their job.
Bruce |
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Registered
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Quote:
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Schleprock
Join Date: Sep 2000
Location: Frankfort IL USA
Posts: 16,639
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Premature valve guide wear on the 3.2L engines is very common. Nothing out of the ordinary to see an engine that needs them as early as high 50K miles. I have had two engines that needed them. Both were 60K mile engines when the signs were there- oil consumption and noisy valvetrain.
Intermediate shaft bearing shells seem to hit copper and then level off there. They don't continue to get worse and cause a major failure. It's enough to make you wonder, why bother replacing them since the new shells will suffer the same fate.
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Kevin L '86 Carrera "Larry" |
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